Ted
The pilot formerly known as Twin Engine Ted
- Joined
- Oct 9, 2007
- Messages
- 29,889
- Display Name
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iFlyNothing
I said that I would write a post about the rather insane amount of work the 414 needed to have done on it. I haven't posted about the work much on here, but if you follow Cloud Nine on Facebook there have been a decent amount of updates.
In mid-February when I had my last transport, the left turbo seized up at one of the fuel stops. Fortunately I was able to get it freed to get back home (getting stuck at a fuel stop with 45 dogs would have been very unpleasant...), but it was time for a new turbo. Also, the nose strut was starting to leak, and the aileron bearings had more play than I would like. So a few squawks to get taken care of.
Unfortunately once we dug into the turbo repair, we found a bunch of rivet heads that had come off of the canted bulkhead (a structural item that supports the turbo) and an improper repair that had been done on the engine beam following very significant corrosion caused by an exhaust leak. End result was the airplane needed a new engine beam, which is a huge job on the 414, and a rotten one at that. Hundreds of rivets need to be drilled out and rebucked. Of course, the engine has to come off as well for the job - that's the easy part!
While getting into it more, the exhaust aft of the "risers" (exhaust parts coming off the cylinders) on the left engine was showing signs of age, and needed to be replaced.
RAM Aircraft orchestrated a sponsorship between them, DART Aircraft Parts, and Aerospace Welding Minneapolis, Inc (AWI) to donate the required exhaust bits, which was huge for us as these parts are not cheap. RAM is perhaps best known for their aircraft improvement STCs on Twin Cessnas, which increase horsepower and gross weight, but they also have a number of STCs, PMAs, and products for other aircraft.
The work progressed and eventually led into annual, which we did as an owner assist, the first time I've been able to be more heavily involved in the wrench turning on an annual for any aircraft I've owned or (in this case) managed. It was nice to get to have this level of involvement. Really by this point, the annual was a non-event. The left fuel selected needed to be overhauled and there were a couple of other minor items, but for the most part it was just opening and closing inspection panels. We replaced the transfer pump for the right side nacelle tank which was dead (1 of 10 fuel pumps on the plane), bringing the fuel capacity back up to 203 gallons.
Another big thing I worked on was installation of the LED lights. Aveo Engineering donated LEDs for the plane. We put LED nav/strobes in the tips, an LED nav/strobe in the tail stringer, and LED taxi and landing lights. The installation on those was straightforward. I'll make another post with a PIREP, but the summary is WOW! The landing and taxi lights are the brightest I've ever seen, period. Eventually I'm going to remove the tail beacon and belly strobe, but there are some approvals around those that have to happen first.
I also went through and removed a bunch of unused avionics and equipment. In the end, I removed about 30 lbs or so, including 4 antennas (two of which were big and bulky, adding significantly to drag). Now when you look at the belly from the wings on back, it's completely clean. I'm really happy with that, and it seems to have added a couple knots in cruise and some to climb rate, too. More drag reduction to do in the future.
The engines checked out great on compressions and borescopes. The plane got signed off and annual completed in mid-July, with enough time to do a test flight and be ready to make our trip to Oshkosh. We didn't fly into Osh itself since I didn't think it was wise to fly into Osh for the first long trip out of maintenance for the plane, but everything went well on the flight. At 19,000 ft we were seeing 200-205 KTAS, the cruise climb rates were better than I expected, and the pressurization works great.
Really when you look at it, the engine beam and the exhaust were the big items. The engine beam wasn't expected, but it's never surprising on one of these planes to find some big ticket item at some point. The exhaust I knew we'd have to do at some point on the left engine. Eventually we will on the right engine as well, although it had some newer components on it and is in overall better condition.
It's been a lot of work the past year and a half (and there's more to come), but I'm really happy with where the 414 is now. Most of the accessories on it are new at this point, the engines are doing well, the props are brand new. We've taken out about 150 lbs total from the plane since we acquired it. I think there's another 50 lbs or so to go, although one of the safety/performance/efficiency upgrades I want to do (strakes) will add a few pounds. It ran book speeds when we got it and is running around 5-10 knots faster than book depending on altitude now, at least for the 31"/2300 RPM power setting we use. Most of that is in the MT Propellers, although some of it is in the antenna removal and weight reduction.
The short list items are getting the air conditioning working again (you really notice it being inop on a pressurized aircraft in the summer), removing the tail beacon and belly strobe (once we can get the approval on that), and there are some other accessories I want to replace as preventative maintenance items. Those will be ongoing as we are able. If we can make it work, I do really want to put the strakes on for the safety and efficiency benefits that go with them, but those may be further out in the future depending. Avionics will come as well.
With a cabin class pressurized twin, you're always in a state of continual restoration. When you started with a project in the first place, that state just can be a bit more extreme
In mid-February when I had my last transport, the left turbo seized up at one of the fuel stops. Fortunately I was able to get it freed to get back home (getting stuck at a fuel stop with 45 dogs would have been very unpleasant...), but it was time for a new turbo. Also, the nose strut was starting to leak, and the aileron bearings had more play than I would like. So a few squawks to get taken care of.
Unfortunately once we dug into the turbo repair, we found a bunch of rivet heads that had come off of the canted bulkhead (a structural item that supports the turbo) and an improper repair that had been done on the engine beam following very significant corrosion caused by an exhaust leak. End result was the airplane needed a new engine beam, which is a huge job on the 414, and a rotten one at that. Hundreds of rivets need to be drilled out and rebucked. Of course, the engine has to come off as well for the job - that's the easy part!
While getting into it more, the exhaust aft of the "risers" (exhaust parts coming off the cylinders) on the left engine was showing signs of age, and needed to be replaced.
RAM Aircraft orchestrated a sponsorship between them, DART Aircraft Parts, and Aerospace Welding Minneapolis, Inc (AWI) to donate the required exhaust bits, which was huge for us as these parts are not cheap. RAM is perhaps best known for their aircraft improvement STCs on Twin Cessnas, which increase horsepower and gross weight, but they also have a number of STCs, PMAs, and products for other aircraft.
The work progressed and eventually led into annual, which we did as an owner assist, the first time I've been able to be more heavily involved in the wrench turning on an annual for any aircraft I've owned or (in this case) managed. It was nice to get to have this level of involvement. Really by this point, the annual was a non-event. The left fuel selected needed to be overhauled and there were a couple of other minor items, but for the most part it was just opening and closing inspection panels. We replaced the transfer pump for the right side nacelle tank which was dead (1 of 10 fuel pumps on the plane), bringing the fuel capacity back up to 203 gallons.
Another big thing I worked on was installation of the LED lights. Aveo Engineering donated LEDs for the plane. We put LED nav/strobes in the tips, an LED nav/strobe in the tail stringer, and LED taxi and landing lights. The installation on those was straightforward. I'll make another post with a PIREP, but the summary is WOW! The landing and taxi lights are the brightest I've ever seen, period. Eventually I'm going to remove the tail beacon and belly strobe, but there are some approvals around those that have to happen first.
I also went through and removed a bunch of unused avionics and equipment. In the end, I removed about 30 lbs or so, including 4 antennas (two of which were big and bulky, adding significantly to drag). Now when you look at the belly from the wings on back, it's completely clean. I'm really happy with that, and it seems to have added a couple knots in cruise and some to climb rate, too. More drag reduction to do in the future.
The engines checked out great on compressions and borescopes. The plane got signed off and annual completed in mid-July, with enough time to do a test flight and be ready to make our trip to Oshkosh. We didn't fly into Osh itself since I didn't think it was wise to fly into Osh for the first long trip out of maintenance for the plane, but everything went well on the flight. At 19,000 ft we were seeing 200-205 KTAS, the cruise climb rates were better than I expected, and the pressurization works great.
Really when you look at it, the engine beam and the exhaust were the big items. The engine beam wasn't expected, but it's never surprising on one of these planes to find some big ticket item at some point. The exhaust I knew we'd have to do at some point on the left engine. Eventually we will on the right engine as well, although it had some newer components on it and is in overall better condition.
It's been a lot of work the past year and a half (and there's more to come), but I'm really happy with where the 414 is now. Most of the accessories on it are new at this point, the engines are doing well, the props are brand new. We've taken out about 150 lbs total from the plane since we acquired it. I think there's another 50 lbs or so to go, although one of the safety/performance/efficiency upgrades I want to do (strakes) will add a few pounds. It ran book speeds when we got it and is running around 5-10 knots faster than book depending on altitude now, at least for the 31"/2300 RPM power setting we use. Most of that is in the MT Propellers, although some of it is in the antenna removal and weight reduction.
The short list items are getting the air conditioning working again (you really notice it being inop on a pressurized aircraft in the summer), removing the tail beacon and belly strobe (once we can get the approval on that), and there are some other accessories I want to replace as preventative maintenance items. Those will be ongoing as we are able. If we can make it work, I do really want to put the strakes on for the safety and efficiency benefits that go with them, but those may be further out in the future depending. Avionics will come as well.
With a cabin class pressurized twin, you're always in a state of continual restoration. When you started with a project in the first place, that state just can be a bit more extreme