Ted
The pilot formerly known as Twin Engine Ted
- Joined
- Oct 9, 2007
- Messages
- 29,923
- Display Name
Display name:
iFlyNothing
The annual on the 310 took a while, but we got a lot done.
- New pilot's side window. Old one had a crack in it which, although it was repaired, whistled while flying and leaked cold air in. It got very annoying (mostly the whistle)
- Autopilot was banking 45 degrees all the time in whichever direction. Turns out that the connector on the #2 AI which feeds the AP was loose. This explains why, after the Aspen install, it never seemed to work quite as well as I thought it should. The GPSS roll steering is beautiful now, whereas before it seemed like it was far more abrupt than it ought to be
- 530 upgraded to 530W. Shot the WAAS approach into Williamsport. Works great, integrates with the Aspen beautifully. And I like having the terrain warnings
- Transponder (Collins) was giving issues squawking the wrong code. Cleaned the contacts in the transponder, working well now after two test flights talking to ATC
- Left main tank had developed a slight leak, discovered during inspection. Resealed
Test flew it today - works beautifully.
Next to get the radar and stormscope installed...
- New pilot's side window. Old one had a crack in it which, although it was repaired, whistled while flying and leaked cold air in. It got very annoying (mostly the whistle)
- Autopilot was banking 45 degrees all the time in whichever direction. Turns out that the connector on the #2 AI which feeds the AP was loose. This explains why, after the Aspen install, it never seemed to work quite as well as I thought it should. The GPSS roll steering is beautiful now, whereas before it seemed like it was far more abrupt than it ought to be
- 530 upgraded to 530W. Shot the WAAS approach into Williamsport. Works great, integrates with the Aspen beautifully. And I like having the terrain warnings
- Transponder (Collins) was giving issues squawking the wrong code. Cleaned the contacts in the transponder, working well now after two test flights talking to ATC
- Left main tank had developed a slight leak, discovered during inspection. Resealed
Test flew it today - works beautifully.
Next to get the radar and stormscope installed...